Status | |
Date | Wednesday 11 July 1990 |
Time | 16:00 LT |
Type |
![]() Cessna P210N |
Operator | Private |
Registration | N4618K |
MSN | P21000238 |
Year of manufature | |
Engines | Continental TSIO-520P |
Crew | Fatalities: 0 / Occupants: |
Passengers | Fatalities: 0 / Occupants: |
Total occupants | Fatalities: 0 / Occupants: 2 |
Aircraft damage | Substantial |
Location | Renton, WA ![]() |
Phase | En route |
Nature | Private |
Departure Airport | Chehaus, WA (KCLS) |
Destination Airport | |
Narrative | DURING A PLEASURE FLIGHT, THE PILOT HAD JUST CONTACTED THE TOWER FOR LANDING WHEN THE ENGINE SUDDENLY QUIT. THE PILOT ATTEMPTED AN UNSUCCESSFUL RESTART THEN INITIATED A FORCED LANDING. DURING THE LANDING APPROACH, THE AIRPLANE CONTACTED TREES AND SHRUB BRUSH. DURING THE ON SCENE INVESTIGATION, THERE WAS NO FUEL NOTED IN THE LEFT WING NOR WAS THERE EVIDENCE OF FUEL LEAKAGE. THE RIGHT WING OUT BOARD SIX FEET OF THE TIP HAD BEEN BROKEN AWAY AND FUEL WAS NOTED LEAKING FROM THE WING. THE PILOT STATED THAT HE HAD SWITCHED FROM THE LEFT FUEL TANK TO THE RIGHT MINUTES BEFORE THE ENGINE QUIT. DURING THE ENGINE INSPECTION THERE WERE NO NOTED MECHANICAL FAILURES OR MALFUNCTIONS EXCEPT THAT THE LEFT MAGNETO CAPACITOR WAS NOT FUNCTIONING WHEN IT WAS BENCH TESTED. Probable Cause: LOSS OF ENGINE POWER DUE TO FUEL STARVATION. THE CAUSE OF THE ACCIDENT WAS THE PILOT DISPLAYED POOR INFLIGHT PLANNING BY NOT ADEQUATELY FOLLOWING PROCEDURES OR DIRECTIVES ASSOCIATED WITH FUEL CONSUMPTION. |
sources
NTSB SEA90LA127ACCIDENT INVESTIGATION
Final report
Investigating agency: NTSB
Report nr: SEA90LA127
Duration: 2 years and 2 months
DOWNLOAD REPORT